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Back to December 2003
01-Jan -2004 Working hard on the new acceleration calculator.

Replaced rear wiper motor because the case has been cracked ever since the respray. After months of trying to obtain a replacement somebody gave me two of them. Fitted one, but it didn't work. Fitted the other and it did work.

08-Jan-04 A few people have driven my car recently and most have commented about the brake pedal not biting and seeming a bit squishy. I've been a bit disappointed with it too for a while. However, the brakes do work really well once you push hard enough.

Yesterday, on the way into work, after stopping at the barrier I pulled into the car park. The brakes felt loads better. A slight pressure and they were biting. I was pretty pleased. Until I realised that the handbrake was half on. On the way home I experimented with this. Truth be told is that the handbrake needs adjusting. It has to be pulled all the way up to stop the car, and any sort of handbrake turn manoeuvre is out of the question since all it does is gradually slow the car. I found that having the handbrake lever pulled half way up seemed to make no difference to the coasting speed.

Just makes me wonder: if I fix the handbrake cable tension will the brakes feel better? I guess that when I push on the pedal then the rear drums are having to expand that bit more and that's what's wasting the travel. So the handbrake cable tension is more important than I used to think.

09-Jan-04 The sunroof has been dripping water onto the seats again. I'm bored of this now. On the positive side: we're fitting the roll cage next week.
10-Jan-04 Went round to scrap yard and acquired another sun roof gutter. Temporary solution to the water leak problem. For the long term solution I'm going to cut the roof out of another Astra and bond it over the hole.
12-Jan-04 Fitted the second sun roof gutter. The steering wheel has been feeling loose. Seems that the whole column is rocking around. The flexi joint is all loose again. Hmm, feeling a bit bored with all this hassle. On the plus side, I have had some good times out on the road.
13-Jan-04 Day one of roll cage fitting. Rob Fairbrother (Vaux MD group) and myself spent the whole day in the workshop. A lot of time was spent on preparation - removing paint and seam sealer. We also bolted the whole cage together to make sure it would all fit properly. I expanded the car slightly with a hammer and punch since the rear arches were closer together in my car than the donor vehicle that the cage came from. The mounting plates were  then tacked into place and the cage dismantled. After a journey out for food and welding gas we got on with the serious welding. There were some good fires as the under seal burnt off. Not so funny when the petrol lines had flames licking over them. By the end of the day the rear cage was fully welded in and the front ready to go in.
14-Jan-04 Day two of roll cage fitting. The front was assembled and the mounting plates tacked in. The front cage was removed and the plates welded in. Finally the front cage was fitted and torqued up. We ran low on welding wire so we did another journey around the world, finishing off with Tescos for essential cakes.

We bought the steel for future additions to the cage. Due to lack of time was had to do some MOT remedial welding. A small plate in the sill in the driver's footwell. The driver's side rear turret was then tackled. This had some rust breaking through. After cutting the top layer off the turret the underlying Steel was found to be sound. So we made up a new plate for the top and welded that in. Rob then seam welded the turrets on the inside and outsides.

After that we cleaned all the welds up and primered the internal welds and undersealed the exterior welds. It was about 8pm by this stage.

Finally I had to sort the rear drums out. After removing the driver's side drum I found that the auto adjuster was jammed on the minimum setting. The mechanism was cleaned out and greased and then adjusted. The passenger side drum was found to be self adjusting. The whole lot was reassembled, the shocks refitted and the car finally lowered.

We finished everything by 11pm.

15-Jan-04 MOT day. Few odd jobs: new wiper blades, proper brake fluid reservoir sensor from scrappy, oil, water, screen wash top up. Car washed. Car dropped off at MOT garage.

Two hours later I phoned up for the bad news. Nothing serious: headlamp loose, one side repeater not working, indicator stalks loose. Luckily I had some spare headlamps in the garage. With the indicator problem I went to the scrappy again and obtained another assembly. But that was just as loose. So I wrapped tape around the bungs that hold it together and that solved the problem. The side repeater problem appeared to be a bulb failure. But it wasn't. As I set to with the multi meter it was dark, cold and starting to rain. Oh well, on the final straight now. After half an hour I found that the problem was a dodgy contact on the multi plugs in the passenger footwell.

Back round the garage and finally I had myself another year's MOT.

17-Jan-04 Finally sorting the sun roof problem. I went to the scrap yard with a rechargeable jig saw and a hammer and chisel. I cut the entire front section of roof out of a non sun roofed Astra. Both rechargeable batteries were flattened in the process, so I ended up using the hammer and chisel which wasn't that difficult really.

Back at base I drew the required outline on the panel and then cut it out with an angle grinder. By being careful I got most of it right first time. I cleaned it up with a file. Then the real problem was tackled: there was a massive tar patch stuck to the underside of the roof. Removing this was alright, but it left a large amount of glue which I couldn't shift. In the end I loosened it with solvents and scrubbed it with Scotchbrite. Then I used a wire brush on a drill to spread it around and finally more solvents. It took ages. The panel looked pretty good on the car. Then I noticed some dents where the screwdriver I'd used to remove the tar had made dimples in the metal. I ground most of these down and then sprayed the panel with primer. I decided to get the body shop to paint the panel properly.

22-Jan-04 The roll cage has made a really good difference to the way the car corners. The back seems to dig in much more firmly and predictably. I guess that the shell was flexing before.

The brakes are massively improved now that I sorted the rear drum tensioner out. The car does not pull off line at all when I brake from high speeds.

25-Jan-04 I went to Santa Pod drag strip. After staying up to 2.30am helping sort another car out I didn't get up until midday. I made it to the Pod at 3pm after some excellent fun on some mildly slippery roads. I  managed to get two runs in.

The last three times I've been there I've managed low 15s at around 92mph. Since then I've changed the bottom end and added some weight. I did two runs. A 16.9 and a 17.1 both at around 88mph. That's about 4mph down on previous results. Both times I span the wheels to buggery. I changed into 2nd at 3000rpm in an attempt to overcome the problem somewhat.

I've run the results through the acceleration calculator and they tally up if I limit grip to 0.35g, rather than the 0.7g my car is capable off. So that means the wheels were slipping in 1st and 2nd gears.

On the way home I was wondering whether I might have lost power, but I don't think so. The car feels as fast as ever (Book of excuses, chapter 1 "it's a goodun"). Allowing for the cage and maybe a few missing hp due to cam timing (chapter 2, section 2, "little things that all of a sudden make a huge difference") then I reckon it should be capable of the mid 15s. The extra 1.5s were made up with a 0.9s delay getting to 60ft (3.2s compared to a more typical 2.3s) and a few more tenths in getting to the 1/8th point.

Therefore I primarily blame traction. I don't think the uprated clutch helps, since I could slip the old one a bit better (Chapter 3, "I was having a bad day").

Anyway, I intend to return when it's warmer and I can get more runs in. I've done some shockingly bad times before.

06-Feb-04 The rear exhaust rubber mount snapped. Need some TAS uprated engine mounts. The sunroof panel is ready to go in. At last. Other than that, just driving the car and saving money.

I'm spending most of my time helping Rob Fairbrother with his Astra GSi turbo project. It's totally stripped out, caged, tuned turbo engine. The shell is finally finished now and the bits are being fitted to it.

09-Feb-04 Finally ordered some up rated engine mounts from TAS. Also ordered a steering knuckle joint. This replaces the flexible joint between the steering column and the rack. The standard ones aren't up to the job. They lose their stiffness after a few months.
11-Feb-04 Steering knuckle joint arrived. It had splined holes. I needed these machined out to accept the flat on the end of the steering rack. Looking at it, I reckoned that I could do it with a file. One and a half hours later I had it fitting on a spare rack. Impatient to see what a difference it would make I couldn't resist fitting it. So I took the steering column and the flexi joint out.  I was busy putting it back together when I realised that the steering column also had a flat on it rather than being splined. Since everything was in bits I decided to file the other end of the joint out as well. Another one and a half hours later it was time to put it back together. What an arse ache it was. I ended up lying in the footwell with my feet in the air on the driver's seat and my head on the brake pedal.
12-Feb-04 Took the steering steering apart again and did some more filing. Because I hadn't aligned the centre of the joint with the axis of rotation, when I turned the wheel the steering column was trying to move relative to the mounts. All sorted after some artistic filing.
15-Feb-04 The joint has made a noticeable difference! The car feels ace.
21-Feb-04 Migweb/Vaux MD mate Pete came round and we spent the afternoon doing some jobs on his stripped out Nova. New track rod ends, new rear brake cylinders and braided brake hoses. Then we fitted new track rod ends to my car. Finally I refitted the bump steer mod.
24-Feb-04 The new track rod ends hadn't solved Pete's clunking. So we had another look. Turned out to be a spring out of its seat that was catching on the spring cup. After that success we felt buoyed up and got on with the tedious task of bleeding my brakes out.
28-Feb-04 Finally got round to wiring in the oil temperature sensor. I arranged a two way switch so that I could toggle between water and oil temperature displayed on the standard digi dash.

Removed the bump steer mod. It didn't seem to improve the steering. In fact it made things worse. I'm not sure why. I think it was to do with the loads acting to twist the rack internals.

29-Feb-04 Today I went mountain biking which was a good excuse for a scenic drive. Woo hoo does the car feel good now! The way it pulls from 4K up is very satisfying, the noise is great, and the steering feels really direct. I was having a great time on the corners. The road surface was in top condition for some controlled drifting brought on with some lift off over steer. Wedged into the bucket seats it felt really good. As much fun as its ever been. I finished off tonight with a full on, old timer style scenic excursion. That included doing one bit of road three times (forwards, back and forwards again), a proper pointless detour that added another hour and loads of whooping at the cheeky way the front grips on fast corners.
14-March-04 Generally not spending money on the car. Still enjoying driving it as much as ever. Went on an Evo forum meet today in Wales. After a sub aqua start with a scary aqua planing moment on a bend the weather improved. Some favourite B roads were travelled. Mid afternoon we came out on the A44 and I hit a real flow. The road was slightly damp, there was no traffic around and I really got into the flow. The car corners beautifully, a slight lift off once on a bend brings the back round. It was so good. As well as a new bit of B road, some classic old favourites were taken on the trek back to Gloucester.
17-March-04 Fuel leak from petrol filler cap has returned. The metal is a bit corroded and stops the cap from sealing properly. At least I know what it is, as opposed to the mystery of the fuel smells from last year.

New rotor arm and distributor cap as the engine has been a bit jerky at low rpm.

20-March-04 Not much is happening at the moment. I'm repaying debts. It's going to take a few more months before I'm ready to start spending on the car again.
6-April -04 The Astra is now off the road for a week.
Rob Fairbrother (MIG and Vaux MD) and myself are doing some major structural work.

Full story.
 

22-April -04 The car is now back on the road.
22-April-04 Feeling pretty chuffed with myself at the moment. First up, I regard the Astra as reasonably fast, I can manage low 15s on the 1/4 mile, so it's similar to a Clio Cup 172. 0-60 is just under 7s based on the 1/8mile speeds on the drag strip. It's only got 145BHP but it is light and geared down for acceleration. So it's good from 15-80ish but it's going to fall behind more powerful cars past 100mph. Anyway, here's some recent experiences that have made me chuffed.

On Sunday I had the pleasure of following a Boxster S down some twisty roads and was keeping up without having to work too hard. This includes corners and straight lines. Now, bearing in mind that a Boxster S is capable of a 14.2 1/4 mile this seems just about plausible. The RWD set up gives it a 0.5 or 0.6s advantage on the launch, so we're only talking 0.4s difference on a 1/4 mile which is not going to be noticed when tackling a load of bends and short straights. All the same, I was chuffed.

An Elise was getting away on the straights. I was pondering the power to weight balances of the two cars and concluded that the Elise must be a sport 160 or similar. At a stop I found out it was a 190BHP new model. Talk about feeling pleased, the driver confessed that he was surprised I was keeping up. It did involve a bit of fear though.

So there you go, recent performance comparisons on twisty roads have shown that a 145BHP 8v engine is enough to keep up with some expensive machinery and still have a great time.

25-April-04 I went to Castle Combe today. I got up a bit late because I was knackered after last night. I finished off some jobs on the car, like Waxoyl cleaning up, side skirt on sticking and putting some fuses back, I went down to Protyre to have the tracking done. They had a one hour wait, so I decided to head onto the Combe, hoping to arrive before midday.

Once I made it the Combe I went to buy track passes and could only get 4.15 and 4.45. So that gave me a few hours spare. Enough time to get the tracking done, so I went down to Chippenham to find a Crapfit or similar. After driving around for a while I found Halfrauds and went to see what they could do. Nothing, but they did tell me where Crapfit was. Sort of, the instructions sort of made sense, so after a bit of randomness I stumbled across Crapfit. They were very friendly there, but told me to come back an hour later. So I went to sample the wonders of Chippenham. After a long Coffee and some newspaper reading I made it back to Crapfit for 2.30. They were very interested in the car so I spent a good while chatting to them whilst they sorted the tracking. The angle is supposed to be -1.5 or something. So +12 was probably a bit out then. I knew the tracking was out. It wore my previous tyres severly on the inner edge.

By the time I got back to the Combe I only had 30 minutes before going out on track. I had a few passengers lined up, but couldn't find them. I guess my late track time and me not being there most of the afternoon had confused them.

On track things were OK. My first session was used remembering how to drive on the track. I got stuck behind a Golf that wasn't any faster or slower than me, and it was a tad dull because there was little overtaking. The brakes were working really well which was nice. The oil temperature was +4 bars all the way round. It normally peaks at +3 bars, so the oil cooler was probably useful, I might refit it.

My second track session was loads better. I reeled a few things in and had some sort of proper Porsche following that I seemed to leave behind on the bends. I couldn't gain on a 106 Ralleye though. The kit cars were really fast, apart from one that I overtook, wonder what engine it had. The Z3 M was being driven slowly on this session. I was pretty annoyed by stupid behaviour on the track. I overtook someone on a straight, then had to slow down to follow the car in front round the corner and the car I'd overtake came up on the inside of me. WTF? I did have a far better time on the second session, I was starting to flow, taking better lines, not being pressurised by other people, and my initial fear at the increased levels of oversteer was turning into pleasure at how the oversteer could be balanced on the throttle and used. I stil don't think that I was comitting myself enough, especially on the big corner by the pit lane.

We then had a scenic drive home. Pete and myself did some good A and B roads. On the hill out of Nailsworth into Horsely my battery warning light started to flash. Then the ECU light came on and off a few times. Then the engine started to misfire. I kept on driving. Then I had no choice because the engine was dying on me. So I pulled over.

I got out to have a look and there was smoke coming from under the bonnet! I gesticulated to Pete. We opened the bonnet and a massive flame shot up in the air. It was coming from the gearbox end of the engine, near the fuel lines.

A bystander was watching and gave the encouraging words "that's gone mate, I'd get back if I was you". Me and Pete rapidly closed the bonnet. WTF to do? In a mild panic I had a look around. Across the road was a coach yard and there was a tap and hose pipe. We both had the same idea at the same time and ran across the road. The hose had some silly brush on the end, but it was better than nothing. I opened the tap and ran back to the car . We opened the bonnet and again there were loads of flames. It looked like more. I had a feeling of fear laced with dread. The car was going to burn. I'd be left with nothing but a shell. The water coming from the brush was not enough to stem the flames. We shut the bonnet on it and ran back.

We watched from the other side of the road. Nothing much was happening. I went to the tap and opened it all the way, it was only about half way due to the rush. A bit of smoke still, but not no more than before. Feeling a bit more confident I got a screw driver out and removed the jubilee clip holding the pipe to the brush. Water gushed out. I opened the bonnet and doused the flames in torrents of water. It was working. Shortly there were no flames. I continued to spray the engine area for five minutes.

By this time the fire service had arrived and looked a bit sad at the lack of fire. The police turned up too and were friendly enough. They saw that I'd been to Combe Castle and were joking about thrashing it. As they talked to me I assesed the damage. A load of wiring loom had melted. But once I pulled the molten tape off it, most of the wires were OK. I reckoned we could start the car.

The lady whose hose it was turned up. She was OK about the drama and packed her hose away. The fire service and the police went. It was just Pete and me. I seperated all the molten wires and cut some of them out. I tried to start the car and Pete connected some loose wires to the live. The engine started. The fuel lines were leaking though, leaking like a shot gun riddled Mickey Mouse cartoon character.

We had various suspicions as to the cause of the fire and what had happened. The most likely was that the braided fuel hose had been chafing on the wiring loom and had finally cut into a permanet live wire from the starter motor. The heat had built up and ignited the insultation (aka insulation) tape and cable ties. Once this lot got going then the fuel pipe was heated up until finally the inner of the pipe melted and there was free fuel to fund the fire.

The thing is, we had installed the pipes late at night and I was left with the job of tying it all down and making it safe. I wasn't too much a fan of cable ties, so I left it pretty much how it was. So, today was an education as to what can happen when an earthed hose crosses a wiring loom.

It was time to call back up. When you've got a job and need help you call the Vaux MD rapid reaction vehicle. Aka Philastrasport. Whilst waiting for him we rolled the car back into a covered busport on the other side of the road. The lady and her fit ish daughter brought us Coffee. Once Phil had arrived then we set to replacing the fuel pipes. After getting them on the right way round and having Phil do some wire and tape work then the car started. Only I had a permanently operating fuel pump. It was enough to get me home though. I though I might as well carry on driving as I had before.

Anyway, the overall damage is a slightly molten scuttle panel, some melted wire insulation, some paint burnt off the inside of the bonnet and a pain blister on the top of the bonnet. My pants survived, though I really did think the car was going to be burnt out at one point. How lucky was I in stopping right by a hose pipe? I'm ordering a large fire exstingisher on Monday morning.

Back at the garage I had a good look at the mystery wires that had been cut off and sorted out what had to be connected where. Only it didn't work. I suspect that the fuel pump relay is knackered because it's getting 12v but only putting out 0.3v. As Pete said, though, there's not many people who drive a car away from the site of an engine fire.

28-April-04 I've been suffering from wobbly vibration at highish speeds. I suspect three things: CV joints, wheel balance or brake discs. Since we broke one CV joing when removing the drive shafts, I decided to replace the other three. Starting at 10pm and finishing at 1am. Like the bad old days.
29-April-04 Well, the car feels a bit better, but the wobble is still there. I might swap the front and rear wheels next. If that doesn't work then it's probably the brake discs, since these were cooked when the brakes seized on and I boiled the brake fluid.
2-May-04 Some jobs need doing. I'm having to disconnect the battery every time I leave the car so that the fuel pump isn't left running. The central locking ECU needs replacing, so I have to unlock the car by climbing in through the back (delocked doors). The fuel smell is still there. Last time I looked, I was convinved that there was a crack in the filler neck, caused by my hammering the metal flat. The wheel wobble is still there. Also, since doing the CV joints, the car seems to wander a bit on bumps. Going to check the suspension. It's running well though and I'm still being entertained.
8-May-04 Action day: bought some spray cans of underseal. There's some patches where the seam sealant was burnt off during welding. Bought new fuel pump relay and battery. Finally went to the scrap yard to get a replacement fuel filler pipe and windscreen wiper motor. The existing wipers have worn through the bushes, so there's loads of play in the wipers. I also lost most of the bits during the welding, so a cable tie is holding one of the parts on.

At the workshop I sorted the fuel pump relay and battery. Everything worked fine. Then I sorted the wiper motor.

Suspension inspected. Found an extra washer on one wishbone bolt. Then realised that it was a driveshaft washer, which I'd put in the wrong place last week. Remember, tiredness causes mistakes.

I cleaned up and painted several areas under the car.

I found that the fuel filler pipe had indeed cracked where I'd been hammering. The metal around the filler neck was also a bit rusted and manky. Even though it was late at night I was up for some creative plate cutting. I cut some Aluminium  plate to fit in the recess on the wind, with suitable holes for the filler neck and screws. After some QRust treatment, I bonded the plate on with Glass Fibre filler.

12-May-04 Things are a bit quiet at the moment. As usual, I'm trying not to spend money. I'm having continuous problems with a petrol smell in the car.
17-May-04 Took petrol tank off and inspected it and all of the pipes. Nothing wrong was found. Then spent a long time refitting the tank and pipes.
28-May-04 The uprated engine mounts are at last available! I've been waiting since February.
29-May-04 Quick oil change. The sump gasket it leaking. And the gearbox. And the petrol tank. I've found a small leak in the tank. That might explain the smell.
02-June-04 I fitted the rear TAS engine mounts tonight. When I first started the car I thought that I'd done something wrong, such was the noise. On the road the increase in transmission noise and engine vibrations was immediately obvious. On the plus side, the car feels loads better. The gear change is no longer sloppy, it seems to go round corners more smoothly and pulling away is improved.
03-June-04 I had to fix the petrol leak this morning. The rate of drippage had increased over night to an unacceptable level. So I drained most of the fuel out and blocked the seepage with body repair glass fibre filler.
07-June-04 Extensive on road testing in Wales this weekend has confirmed that the mounts have improved the handling/traction noticeably. Along with 4 new tyres, the car was an absolute blast. As good as ever. I'm so buzzing, the handling is so intuitive and entertaining. The road from Sennybridge to Llandovery was awesome. So many corners. The lift off oversteer is spot on. Big grins all round.

The noise is quite extreme with the TAS mounts. The whole shell, being totally stripped, vibrates like a big drum, especially on the over run. Brought a big smile to my face. It's bloody ace. I'm really impressed.

07-July-04 Things are quite quiet on the modding front (unlike being inside the car). I'm still not spending money. I've been doing a lot of driving and it's as much fun as ever.

I've been helping a friend fit a tuned up 2.0 8v engine to a Scirocco. Big valves, big cam and twin 40s. I'm interested in how it runs and how many mpg it manages. I could be tempted.

We were down at a really good rolling road tuner (Car Improvements near Yate) today. He was very interested in my car and had some good ideas for improving the engine quite cheaply. A manual distributor would allow him to adjust the ignition timing and he though that could allow better output from the engine. He also said that rising rate fuel regulators (like the FSE Power Boast (sic) valve) did work on some engines. I was quite tempted by the idea of fitting a fast road cam, manual ignition, a vernier pulley and adjustable fuel pressure regulator and then getting him to optimise it.

31-July-04 Still not spending money. Still driving and enjoying the car.

Spent this weekend transplanting a 2.0 16v engine out of an Astra GTE into a Cavalier Calibre (not a Calibra). We took two engines out, swapped a load of bits over and fitted the engine into the Calibre in one late night and one full day. The extras like wiring and welding the exhaust systems up took some of the time. It all ran though after some fiddling around with the electrics.

6-Aug-04 Started work on fitting the seats properly. This entailed removing the seats, bits of the roll cage, the battery box and the fuel tank. Then the original seat mounts were removed. Holes were drilled and tube welded in its place. Full story.
7-Aug-04 Long day in the workshop. Half of the seat rails welded in place and a load of seam welding.Full story.
9-Aug-04 Another long day in the workshop. Got all welding finished. Then the long process of painting all the metal both inside and out. I was on my own by the end and it was a 1.30 am before I had the car finished to drive home in. It was worth it though. The seats now sit 2.5" lower than previously, which is about 1.5" lower than standard seats. Full story.
11-Aug-04 There's been a bit of an oil leak. Inspection suggests that it's coming from the oil cooler sandwich plate.
13-Aug-04 Fitted new O ring to sandwich plate. Hopefully the oil leak will cease now. I'm bored with the smell of burning oil from where it drips onto the manifold.
15-Aug-04 Oil leak seems to be fixed. There's still an occasional smell of burning oil though. This time I think it's a small leak on the rocker cover.

I've acquired a distributer, Hall sensor and ignition module from a 1.8 8v Cavalier. This will fit in place of my current distributer which is controlled by the ECU. My local tuner reckons he can obtain more power by having control over the ignition timing. So the ECU will be ignored.

I've had a bit of worry with the oil pressure this week. It sometimes drops the first bar on the digi display. I've got a few theories, one being the thinner synthetic oil I've tried out.

19-Aug-04 Had a go at fitting the distributer. It fits directly in place of the current distributer. I need different ignition leads, plus I need to wire in the ignition module.
20-Aug-04 I've been studying the Haynes manual and the wiring looks simple enough. I'm also looking for some equal length drive shafts from a Cavalier GSi.
01-Sept-04 I've just won a Kent AST14 cam kit on Ebay. I'm really pleased. Std Sri 130 cam spec is 264 degrees LC 110 22/62 62/22 cam lift 6.0mm, valve lift 10.14. The Kent cam is 272 degrees and 12.64mm of valve lift. Should add a few horse power at the top end and hopefully not lose too much at the bottom. I paid £122 for the kit. List price is £280. Luckily I put in a bid 15s before the end of the auction and outbid another last minute bidder.
03-Sept-04 Good progress was made tonight.

Annoying rattle and wobbly engine was traced to a rear engine mount bolt that was tight in the hole but not actually tight against the mount. That was sorted.

Oil pressure problem was tackled. Pressure relief valve was cleaned out. Pressure sender also cleaned and rewired.

Finally, the 1.8 distributer with Hall sensor was fitted in place of the ECU controlled distributer and coil. Only three wiring connections were needed. Live feed from the original coil live. The ECU coil earth was cut and the ignition module switched earth used in it's place. Finally, the new circuit required an earth wire. After sorting that, the engine was started and it fired into life first time.

Which was nice. We then divved about with the timing a bit.

First test drive has shown that it works fine, you wouldn't notice any difference between that and the ECU driven coil.

The Kent cam kit should be arriving soon. I've got a set of new lifters ready to go in too.

So, all I need now is some carbuncles.

07-Sept-04 Engine died on way home from work. Start of long story. Waved goodbye to the njection system.

Read all about it.

10-Oct-04 Entertaining interlude on Dartmoor.
29-Oct-04 Carbs are great!
06-Nov-04 Spent the evening fitting a proper Dellorto throttle linkage. A very long and involving job. All worked out fine in the end though.
22-Nov-04 Everything is running well. Time for an oil change. New cam belt also ready for fitting since the current one has had a hard life over the last year.

I've acquired a massive 4-1 tubular exhaust manifold, courtesy of a Vauxhall fan in Brazil.

9-Dec-04 Got into car to drive somewhere and the throttle cable snapped! Happened where it connects to the linkage; the wire had fatigued through. I managed to bodge the remains of the cable into the clamp.

I've discovered the source of the burning smell at high rpm. The oil filler cap is leaking oil when the revs are high. This drips down onto exhaust manifold.

11-Dec-04 Had a slow puncture fixed. Turned out to be 2 large nails in the tyre. Oh well.

Car is going so well. Total hoot to drive. I need a rev limiter though. I've been over 7K quite a few times and I've no idea how many rpm I'm doing.

Had a bit of a trip to Wales this weekend. Car is going so well.

19-Dec-04 Bit of a list of things to fix at the moment:
  • New side repeater to replaced cracked one
  • Front wing bolts
  • Fit old crank sensor to liberate decent one that's in there
  • Sort water pipes that still have spark plugs in them as bungs
  • Reattach mesh in front grille
  • Tighten rocker cover bolts
  • Fit new distributer O ring
  • Fit new lower arm bushes
  • Inspect rack and linkages for play
  • Inspect filler cap for leaks
  • Clean and paint a few patches on the front triangulation where paint has come off
  • Finish wiring in car
  • Replace screen wash pump
  • Fit new 4:1 exhaust manifold, with welding
  • Maybe maybe fit brake bias peddle box
25-Dec-04 Washed the car. Started to feel really keen, was going to do some minor jobs but then it started to snow.
26-Dec-4 Still feeling keen. Sorted distributer oil leak. Tightened cam cover bolts since this was leaking oil too. Fitted cut down crank sensor. Sorted screen wash pump out - gauze was blocked.
28-Dec-04 Fitted the 4:1 manifold. Involved some entertaining welding. Story.
29-Dec-04 Phoned up Autovaux for bits to sort the suspension. Looking into brake bias boxes. Phoned up Motorsportparts, they were very helpful and were still willing to help even when I said I think I could get a pedal box 2nd hand.
30-Dec-04 New manifold has improved the engine sound. The carbs seem to "baaarrp" a lot more crisply than before. Also, some proper pops, bangs and pings on the over run.

I called round the tuner's this afternoon. He really liked the look of the manifold. He offered to put it on the rollers right there. So we did. No major fuelling issues. He noted a dip in the torque output at around 5K. We didn't know whether this was a dip or either side was a peak.

With the engine on the rolling road I got to see how much vapour was coming out of the catch tank. Loads of it. Not healthy stuff either.

Now I was confident of the fuelling then I gave the car a proper high rpm work out. I wouldn't say that the manifold has made a significant difference in acceleration. The engine does seem to pull a bit better at from idle, and also seems to pull a bit better above 7K.

31-Dec-04 I did some unscheduled rust proofing today. I was driving along giving it some. When I pulled in at the end there was quite a lot of smoke from under the bonnet. Took a look and the oil filler cap had fallen off. Shut bonnet so that smoke wouldn't turn to fire. Thought about ways to block the hole up. Decided to have another look under bonnet. Filler cap was found down back of engine.

On to January 2005


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